Component Selection
There are a number of alternators suitable for use on a Tiger. The
biggest problem is that it is necessary to mount the thing such that the
belt pulley lines up with the Tiger's water pump and crank pulleys. Because
the Tiger used a non-standard water pump and crank pulley, it is going
to be difficult to find a Ford bracket that will fit the Tiger. Since this
is the case, it is not really necessary to use a Ford alternator at all,
and in fact several Tiger owners have fitted a Chevrolet 45 amp 'one-wire'
alternator. In my case I had an internal-regulator Toyota alternator sitting
on a shelf, and I have used these alternators successfully on a number
of street and race vehicles, so I decided to use it. The Toyota part number
is 27060-28020, and they can be found on 1980-1982 Corollas powered by
the 1800 cc 3T-C engine. The belt tension adjuster brace is Ford part number
C90E-10145-B.
Fabrication
I had to make
a bracket to mount the thing, of course. The alternator mounts using a
10mm by about 5 inches long bolt that goes through two ears on the alternator,
and I had a friend machine up a piece of 1" cold rolled steel bar stock
to fit between the ears. The rearmost ear has a pressed-in distance piece
that allows for slight variation in length so this is easy. I used a piece
of 3/8" steel plate for the cylinder head side of the bracket. Cut it to
a kidney shape, drilled two 3/8" and a 7/16" hole and bolted it to the
head. The left arrow in the picture at left points to the lower (7/16")
bolt in the head mounting plate.
At this point I threw everything in the car and eyeballed the alignment of things. By sheer luck the rearmost edge of the alternator ear bracket (the 1" bar stock piece) lined up with the front surface of the head plate. I then measured the distances from the two 3/8" holes to the bar stock piece, and this gave me enough information to build the stuff inbetween.
I used three ribs of 1/8" steel plate for the stuff inbetween. I cut
out the middle rib (right arrow in the picture above) and welded this to
the 1" bar stock, then welded that to the head plate.
I spent a few minutes after that with a large square to ensure that things
were straight, then tacked the other two ribs into place. Recheck the squareness
again and adjust as necessary. At this point I took stuff home again and
bolted the bracket to the head and the alternator to make sure that the
alignment and measurements were okay. As can be seen from the picture at
right, the dipstick tube was a very close fit and required both a cutout
in the middle and upper ribs, as well as bending the dipstick tube. The
ribs were then boxed in front and rear with more 1/8" plate to ensure a
rigid structure. After that, I cleaned things up with a wire wheel in the
bench grinder, and painted it.
Wiring
For the wiring,
I decided to use the existing harness as much as possible; since I had
to remove the regulator anyway, I used the large brown/yellow wire that
ran from the generator to the regulator, and connected it to the large
brown wires at the regulator side, and to the battery terminal lug on the
alternator. The small brown/yellow wire on the regulator connects to the
dash charge light; I connected this to the brown/green wire that ran to
the generator, then on the generator end I connected it to the "light"
spade terminal. I had to run a new wire from the ignition terminals at
the fuse block (white wires) to the "IG" terminal on the alternator. This
wire is just barely visible (I used a black wire and ran it along the firewall)
in the picture. Feel free to bug me at SUNI if I haven't wired the ignition
lead better yet.
The belt I used was a few inches shorter than stock. Use your favorite brand.