I was going to call this 'let's drop the big one now'. It's the last big project I wanted to do to the car. It turned out bigger than I thought.
During the years I owned the Mustang, probably every component had been re-built or changed except the rear axle, which had been left pretty much stock. Just some urethane bushings, stiffer springs and shocks. The stock Mustang four link geometry was still in effect. This arrangement tends to fight itself and bind up, leading to weird handling.
The aftermarket seems
to have settled on one of two cures. Replacing the upper two links
with either a Torque Arm, or a single Upper Link to make a 3-Link.
There are also other systems, such as a Satchell Link, or the
good old 4-links straight back from the frame. Most types also
need a panhard rod, or such, to locate the rearend sideways under
the car.
The cheapest 3-link is simply to remove one upper arm. People
call this the PM3L, The Poor Mans 3 Link.
Some people call a torque arm a three link. I say a three link
has pivots at both ends and is above the axle center line.
I knew others had built all of these, and debated with myself
one way or the other which one to chose. Any would probably do
the job, and so came to the result that there is no right or wrong.
Looking at it from a practical viewpoint, the torque arm can be installed totally under the car, while the 3rd link requires the temporary gutting of the rear seat area. (some kits require permanent removal of the rear seat.) When completed the 3rd link is up out of the way, but is near the floorpan, while the torque arm hangs down under the axle and crowds the exhaust. The 3rd Link is much lighter than most Torque Arms. But the Three Link is also close to the brake line, while the Torque Arm isn't.
In the 2005 Mustang Ford
changed the rear to a three link. I decided that maybe they knew
something I didn't so finally picked that type. I had the goals
of:
-proper geometry,
-lack of noise and vibration,
-packaging under the rear seat.
In addition the entire axle would be swapped and the stock nine inch drum brakes would be replaced with newer style discs during the operation.
Suspension page first, then brakes on another page.
![]() |
Step One: Build a fence. This is so the garage could be emptied, and the interior of the car gutted, and all the stuff hidden from the passerby. The cut-off tops of the fence posts would also be handy to rest the car on because I wanted it as high off the floor as possible. The neighbors liked it too because it hid their patio from the alley. |
|
First big surprise after the
inside of the car was removed: the back of the car was rotten.
Areas behind the wheels were rusted out and hanging around out
of habit. My car has a rear window washer, and after some poking
under it the top of the tailpipe could be seen through the floor!
Evidence reminded me that I had 'fixed' some of this years ago with the only tool I had; a drill with a wirewheel, and then some fiberglass and bondo. It held together a remarkable time really. |
![]() |
![]() |
The other side was only one third bad, but there were several small holes, and the inner fender wasn't attached to the outer at all. A v-shaped channel was made to weld them back together. It's much easier to do without an axle in your spine. At the back on both sides bolts were welded in pointing into the bumper cover. The stock bumper system required removing the interior to get at the nuts. Now it can be done from underneath. New metal was welded in and primed, truck bed liner in a spray can covered it, then two more cans of undercoat was sprayed inside and under.
|
|
Computer cases are made of surprisingly thick metal. And they don't rust. Welds a little funny though. Came in handy on a sunday afternoon. I could include a dozen pics, but will leave it as is. All together, it seems like more time was spent on rust repair than on the project itself. The rear springs are sitting high right
now. They were found at the wreckers on a Fairmont station wagon.
Two coils were cut to get to this height. The rate was calculated
at 280 lb. Later a half coil was cut and the top sliced flat,
so it's 290 or so now.
|
![]() |
![]() |
Moving on... The third link bracket was made on an
8.8 that was rebuilt and sitting on the garage floor. |
|
Here is a finished picture. Hard to see it with the fresh gloss black paint. Easy to see the three rear tabs. The bad point of welding these on is that the adapter must be lifted to remove the rear cover. But how often do you do that. |
![]() |
![]() |
Here is another pic after after several months of dust. The center tabs are 1/8th, and then doubled up with a washer. Later a thick rod was welded to the edge. I thought a pic was taken but apparently not. Lastly the angle was triangulated
with flat plate and it was finish welded. Between the tabs a
smaller piece triangulated at the back as well. These brakes lines were removed later.
I'm not the greatest weldor, but the brand of wire that was in the machine was giving me problems. I've written right on the machine not to use it again.
|
|
The entire axle had to be replaced before the third link could be installed. I took it apart in pieces after draining. Old gear oil stinks. While it was out I did several 'might as wells'. It is much easier without an axle in the way. The torque boxes were welded up and a plate added across the bottom. I used a bottle jack to snug it up, and the car lifted off the wood blocks without the plate bending. Strong enough. I got sick of looking at the rust after this. (although the 500W halogen makes it look worse.) I cleaned up the loose stuff with power tools and used a touch-up gun to spray a few coats of anti-rust black on everything. |
![]() |
![]() |
The lower arms and springs were given a bath in the rust removal solution. The urethane bushings were removed for this. The rear center bushings were very rusted, and even after cleaning looked more like archeological artifacts than car parts. Looking around the garage two tubes were found that fit together, and the outer one was aluminium. The inner piece was knurled slightly, lubed with anti-seize, and pushed into the outer with a vise. |
|
The axle was put together outside the car. To move it into positon by myself it was put on a board and slid across the floor with my legs. Under the car each end was raised on boards until a jack could get under it. After it was raised I realized the new axle brackets had not been drilled out to 1/2 inch. While doing that it fell off the jack and I had to start again. |
![]() |
![]() |
Yes, I had a panhard bar with a four
link before I knew it was a bad thing. I even had urethane bushings
for a while before I went back to rubber on top. You can see this bracket has been re-worked several times before. |
|
The axle end has this little bracket
bolted to the lower axle bracket. It was sturdy enough before
so it was re-used. In fact when the urethane caused a bind it
was the panhard that bent not the tab. The panhard has ends made from shock eyes. Urethane bushings are used. The one at the frame has an inner bushing with a 1/2 in bolt, while the axle has a 5/8 bolt, because it is held by one side in single shear. |
![]() |
![]() |
Before working on the 3rd link the axle had to be in position. So everything was bolted up and the car was raised lightly off the wooden blocks to put the weight on the axle. To adjust the pinion angle and hold the axle in place without the upper arms this link was used. It is a rear toe link from a Dodge Intrepid. I was going to use it as the 3rd link, but thought it might be a bit spindly. Too long as is but perfect for this job however. There are many sites with info on setting pinion angle and they are all different, and often contradictory. I used a pdf from Steeda, which was at least straight-forward. Two degrees down. I was curious to test drive the car using this as a 3rd link, but nothing else was hooked up. One of you will have to try that. |
|
Finally I could start the project. After two weeks of this and that the rear seat area was cleared out and a cut was made in the floor. All the bracketry was going to be welded in. But when trial fits were made I realized there were no truly flat surfaces in the car. To weld in pieces would require cutting somewhere. While eyeballing things with a 1x1 inch tube, it was set on bolts turned into the seat belt holes. A thought ocurred that the tube could be used and bolted on. And if the rear was bolted in it didn't make sense to weld the front half. So it became a bolt-on project. Kind of a production prototype. The only pic I have was somehow made small with no backup. |
![]() |
![]() |
Here is the tip of the 3rd link peeking through the hole in the floor. I had made the link extra long, so I believed. But the end was right around the center line of the finished bolt hole. This is the only shot of the bare piece. As it turned out the hole is almost the finished size. Three holes have also been drilled above the area for 3/8 bolts. At this point nothing else had been made yet. The entire project was 'do one step, then figure out the next one'. Without coming to dead end. |
|
The link is made from a 1x1 square tube, rubber bushings from a Mustang rack and pinion, and a thick walled tube that happened to be around. The center tube was from the old Energy Suspension urethane upper links. It all fit tightly, and had to be rubber hammered together. Seemed pretty tough. And stiffer bushings are available as replacements if needed. I think the stiffness goes; mustang, taurus, aviator, urethane. Welding this piece was the only part that worried me. If it breaks, major chaos. I vee'd the metal, did a pass, ground it lightly, sandblasted it, and did wider passes twice more. This finally made me totally confident in the finished piece. |
![]() |
![]() |
Here's the axle end. The pieces were put together to mock it up, then the next day they wouldn't come apart and the hammer started to damage the center bushing. So they were painted in place. The rubber bushing was belt sanded down to the width of the center tube. The grooves were filled with marine white grease before final installation. I was surprised by the length, thinking it would be 8 to 10 inches. Finished size was 13 1/4 center to center. Hey ladies, CHECK OUT MY 13 INCH MEMBER!! |
![]() |
|
|
The tops of the muffler hanger pockets were cut off earlier. Now flat metal was welded in. Nice job. Last task of the day. Should have photochopped it to make it look pretty. The undercoat on the other side kept catching fire.
|
![]() |
![]() |
The assembly is shaping up. Two tubes have been welded to the square tube over the seat belt holes. (newer mustangs have bolts on the floor.) Longer bolts are used to hold the assembly in tight for every step. These tubes will also allow the seat belts to be re-installed in the same place. Two tabs are located near each end right over the frame flanges. The finished areas were painted ford engine blue. Didn't think of painting the axle piece this color until it was installed. |
|
The top piece is cut from 3/16
inch plate. Four 7/16 holes were drilled before it was tacked
in place. An angle finder was used to ensure the plate was the
same angle as the car. A piece of angle is welded to the top with plugs and stitches. Three 3/8 are welded in. The finished 3rd link is trying to get into the shot. |
![]() |
![]() |
The side pieces are 1/8th plate. Strips of 1/2 were laying around
so that's what was used. Holes were drilled before they were
twisted into shape and tack welded. Their backs were bent up
simply to close off the box from the outside. |
|
Getting there. Notice the rear of the plate is level with the tube, so any bracket can slide over it if needed. The front piece happened to be made of 3/16, which came in handy later.
|
![]() |
![]() |
The bottom plate was tack welded to the top before the holes were drilled. This way I knew they would align without doing precise calculation. The down side is that they may only fit together one way. All the pieces are made from the same 3/16 plate cutoff that was bought from a metal shop. To assemble the bracket properly,
the bottom plate was bolted to the top plate, while the sides
were bolted to the 3rd link. With the axle raised to put weight
on it, and the pinion angle set, the link was held up and the
sides were tack welded to the top. |
|
While drilling holes for the 3/16 rivets I noticed how thin the sheetmetal was. I thought this might cause vibration and fatigue over time. So an extension with four bolt holes was added along the spine to the crossmember. I wanted to use two smaller tubes but this is what I had, and I had to stick two scraps together to get it. My Three Link has a Torque Arm! |
![]() |
![]() |
Now we're getting somewhere.
Looks better painted. There are 9 bolts, 8 self tapping screws, and 16 rivets holding it to the car. It's not going to tear out anytime soon. I almost forgot to weld in the four top bolts before painting. The width of the crosspiece was three feet. Then I widened it to reach the inner fenders. Then I realized there was nothing there with any real strength, and it was hard to get in and out of the car, so it was cut back down. When measured again, it was three feet. The piece on the passenger side is rust repair. The spring bracket is behind there, and gunk built up between the pieces and rotted out. |
|
3/16 rivets circle the box. Bathroom caulk was added as a seal before final assembly. The seatbelts are re-installed with 3/8 Fine thread bolts and thick washers. Teflon tape was wrapped around the tube to prevent rattles. The sheetmetal had a few cuts from the AngryGrinder that had to be welded up. |
![]() |
![]() |
Underneath, the bracket is installed. While building it, somehow I forgot that a bolt had to be installed. It just barely fit, after it was cut exactly to length. The white around the edges is caulk, while the white in the middle is white marine grease. The black on the link is overspray from undercoating. That bedliner stuff is impossible to get off. MY 13 INCH MEMBER HAS BLACK SPOTS ON IT!! |
|
Getting on with my life... I stuck the camera up above the axle and straightened out the shots in Photoshop. This one is approximately level. There's the bracket with the rod welded to the edge. Looks nicer. Should have welded it in solid, but I went thru 3 lb. of wire as is and my eyes are throbbing. The welding had to be arranged for only a certain amount each day. The bracket in the background is from the old Rancho adjustable sway bar kit. |
![]() |
![]() |
On the frame, you can see there is only
a finger width of space over the link, but it is near the front
pivot. The back would probably hit the floor first. The bracket bolts are long enough to drop the bracket with a spacer. Of course the holes would have to be slotted to keep the same pinion angle. As is, the driveshaft is five fingers below. The top of the axle mount is also about five fingers from the floor, while the axles' rubber snubbers have a hand width. |
|
A shot of all the bottom bolts. The front ones have a strip of plate that conforms to the floorpan.
|
![]() |
![]() |
Here is the rear seat bottom test fitted. The metal brace at the rear will have to be altered before it falls totally into place. The seat back should fit the same as before, but I'm kind of burnt out right now. Lots of upgrades on the car this year. It feels as if I worked on it more than it was driven. |
|
The Intrepid link was removed easily and the axle didn't collapse. So far so good. Next re-install the sway bar kit. The
entire thing was taken off, de-rusted, and painted.
|
![]() |
![]() |
Of eight bushings only one went bad. Pretty good after all this time. A replacement was turned using a front swaybar link bushing. It had to be cut slowly or else the urethane squirmed away from the cutter. The old one was probably that color once. |
|
The sway bar installed. Big U-bolts hold it the axle. These bolts were rubbing on the tailpipes before so they were moved inwards. Teflon tape was wrapped under the bushings. They say this makes it more slippery and prevents wear. I had previously tapped them for grease fittings . The bar is one inch with adjustable ends. The ends were cut down years ago as they hit the frame. Third Link Project completed. But before a drive; brakes. |
![]() |
|
The first few drives revealed a clunk, so the relocated bump stops were cut, but it didn't help. Now I think it is the panhard bar hitting the frame bracket. Using various suspension programs on
the Web the anti-squat came in at somewhere over 100%, which
I found hard to believe. I was thinking it would be about 60%.
One program also said at 1in movement the axle has no RC shift or Toe-In Gain. Cool. But that program also said I had 143% A/S. Another said it was 122%, with very slight RC and toe change. |
|
![]() |
|
|
Finally I realized that
the drawings I based my design on were flawed. Here
is the same basic drawing that was in many Steve Smith stock
car type books. I have altered it on the left hand side. You can see the difference. At 'A' is is about 40% A/S, compared to about 120% at the front axle. I wonder how many people were screwed up by this drawing over the years? You might think that because they used this drawing again and again, Someone Might Have CHECKED THE FREAKING MATH ON THE THING!!! On the other hand, several of these books said 'not to use over 50% A/S', but they were the ones with the bad drawing. If they are re-calculated the other way, their examples are over 100%. So I'm not so far off after all. |
|
|
Here are some programs I downloaded. http://www.performancetrends.com/SuspAnzr.htm A Demo. I used the 99mustang file for some numbers, then glued them into the 3 link file found in Vehicle Specs. It says I have 141% A/S. http://mysite.verizon.net/triaged/files/3LinkV1.0bBETA.zip It says I have 121% A/S. Same numbers used. http://rapidshare.com/files/95118335/carFactorySetupV1.8.2.zip Here's an article on how the calculate CG Height, if you have car scales. http://www.longacreracing.com/articles/art.asp?ARTID=22 I found a program for Torque Arms at; http://www.rossautoracing.com/antisquat.html Using the rather common 48 inch arm the A/S is 162%. Also very high, yet these type are widely used. EVM sells a 3 link, and states
it "...allows for adjustment of the anti-squat from 90%
- 105%.". |
|
![]() |
My own measurements using pencil, paper, and a scale ruler came up with: 115.27% A/S, IC 41in. at 8in. from the ground, at half a tank of gas. [assuming 18in CGH.] So my conclusion is, drive it more and see how theory compares to direct experience. I have driven it on the highway and around town, but only in the snow. If I do need to alter the amount of A/S, then there is room at the axle bracket. The center can come forward and down, as the photo chopped pics shows. Then the frame bracket can be altered, or my member can be shortened an inch. Ouch. |
|
In January unusually warm weather moved in for a week. I used the time to revise the bracketry on the rearend. The clunk had to be dealt with at least.
If both tires hit a big bump at the same time you had to grit
your teeth as it felt like someone hit the chassis with a sledgehammer. Lowering the rear pivot seemed like
a cure for both the AS and the clunk. You can see the old hole still in place. The paint was cleaned off with a cute little sandblasting pistol that looked like a paintball gun, with the sand going into a top hopper. Fifteen bucks. |
|
![]() |
I could only get two blurry pictures
before the batteries went dead. This digital eats them like candy. The weight off the car is on the axle here but the suspension is not compressed. I roughly calculate AS at between 80 and 100%. And there's no big clunk. White grease was placed on the top of the link and axle to see if it transfers to the frame or not. The next day the weather was back in the deep freeze. |
|
But still there was a thump. Different than before though. So when the weather gave me another break I looked again. No grease had transferred. But I saw was the shock bracket was bent. This had happened before but I thought the floor jack had bent it when the axle was lifted, and so straightened it out and carried on. Now it became obvious that it was hitting the sway bar bracket as the axle moved upwards. I had installed the bolt with the nut to the inside and never looked at it closely again. So the bolt was flipped, the bracket trimmed down, and the head thinned down to be sure. Goes to show how you can over complicate something. I was examining the 3rd link and forgot the simple things. |
![]() |
|
Cut to; A few months later. Still
winter. Understeer is definitely reduced. On a few freeway ramps where I used to tug on the steering hard I now almost hit the inner curb. This surprised me. Without the stock bind the 'spring rate' should be lower, which would increase understeer. However, high A/S increases oversteer. So they cancel each other nicely. (they say high A/S is why certain cars are liked by drifters.) |
||||||
|
||||||
|
||||||
![]() |
Updated. Finally got around to putting the rear seat back in. The back fit after adjusting the bolts all the way up. It still touches the bar a bit, but a firm pull makes it clear. [I forgot the cross bar angles up a bit. My calculations assumed it was level.] Actually I finished over a month ago. A tree fell in the front yard and I took some pictures of it. A week later, where the funk is the camera? It had disappeared. I must have left it in the front yard. The Canon A460 was 'free' from
my credit card company. Luckily I had enough points on a different
card to get another one. This time a Sony Cybershot. It took
over a month to get here. |
|||||
|
The seat bottom had to be altered. The
center of the frame was replaced with a rod. It was bent to clear
and welded in after some eye-balling and guessing. Then the stock
frame was cut out. I had better pics in the old camera. A big square of sponge was cut out where it fits over the 3 link box. Anyone who sits there would have a sore butt. The seats are real factory leather. The hog rings were removed and the cover was stretched out and protected from weld splatter. |
![]() |
|||||
![]() |
Finished. Sweet Jesus. Actually it was a easy project, now that it's over. The one annoyance is a random clunk from the spring areas. I think the axle can move so freely the springs pop out of their seats on big bumps. It's a much better set-up than stock. But then almost anything is.
.. |
|||||