Home Page - Hope you find the information useful, do let me know.
Last e-mail
updated:
2 August, 2006
| I invested $3.19 plus an hour of my time to buy a triad and resistor and replace on my Maytag MAH4000 control board as specified here: http://members.shaw.ca/gavb/ I'm happily and cheaply back up and running. Thanks again! MB |
| Mine died Last Friday night. After researching the web a little over
the weekend I decided to open up my 6-7 year old machine which has never
given me any problems before. It is a Model MAH5500AWW. I discovered it
uses the same board that everyone seems to be having trouble with and
R11 is smoked. I will assume it took Q6 along with it but have not confirmed
that yet. Please add this model number to your list and thank you for
the site.
Bob |
| Suggest you call Maytag and ask for help with the bill. 423-559-3480 Nate |
| The local service store is supposed come here on Monday to supply yet
another controller board, and replace the door lock assembly which includes
the wax motor I will then have two spare controller boards with which
to install the ECO, and a spare door assembly that is probably just fine.
I already picked-up the 3.9K 1/4W resistors. Now that I know the suggested
replacement for Q6 I'll hunt for those also. It's amazing all the noise about this product out on the web. There are even class action law suits. I'd prefer just to get the problem fixed, and not join in with the ambulance chasers, but if it helps ... If I can contribute anything useful to your forum, please let me know. Pete |
* THE STAR E-MAIL - THANKS ROY *Saw your "fix" on the Internet for the Maytag Neptune door
wax motor problem. Interesting approach. |
|
I just couldn't see junking the thing yet and buying something else. I found a website (Digi-Key Corp) that is sending me out the several Q6 Triacs at 50 cents each and the 3.9 Kohm resistors. The board itself is a little fried where the resistor burnt but I can probably jumper around the bad spot. The wax motor is only about $12 so I'll probably replace it too if the rest goes well and I get things working. In the meantime, I talked Maytag into providing a new control board, door lock mechanism and Pha kit for the moldy gasket all at half price (The machine is 6 years old and out of warranty). They'll warranty the parts for 2 years once I pay their guy to install it all. Your fix sounds interesting. Not sure where I would put the relay or what relay to buy. I figure it lasted 6 years and I'll have extra triacs and resistors so I should be able to handle another meltdown if it happens. Nice to be able to communicate with someone about this. Wives don't really understand our need to outsmart the machine. Howard |
|
I was pleased to find your chat page comments that should help me fix my Maytag "Moldtune" washer. I can clearly see that R11 resistor and the Q6 transistor are burned out. It sounds to me like you fixed the problem, at least temprarily, by replacing these without replacing the wax motor in the door lock mechanism? Is that true? Your other idea with the relay, etc is too complex for me but I will replace the wax motor or the whole door mechanism if necessary. Thanks for any suggestions or follow-up. Howard |
|
I have pulled your comments off the chat board concerning your Maytag
Chuck |
|
Well it fixed mine! bought triac and the resister @r11 learned to solder (easier than i thought)and got it going in 25 minutes THANKS for your site!!! Fixed my wifes watch while the solder iron was hot LOL Ron |
| I have a model MLG2000AWW. It had the same r11/Q6 problem. Thought you
may want to add it to your list.I stumbled across this site because I
was trying to figure out what the value of R11 is. I like the tip of using
a 600 volt triac. I had been considering putting in a relay prior to finding
this site. I figured the failure was excessive current. I still might
put one in since it is so easy. Maybe you could point out to your audience
that if they do install a relay, make sure and suppress the coil of the
relay with a MOV or an RC "snubber". This would be a good idea
for preventing a high induced voltage from the relay coil when it deenergizes.
This can fry the control circuit. Also, do you know what the value of
R43 is? I noticed that is a little toasty also, but it is still conducting.
It looks like it has something to do with the "end of cycle"
signal on pin 1 of P2 . Very informative site, thank you. Arlen |
|
Another happy customer...Yours, that is! R11 Q6 and the Wax motor in the door... Easy pie. My wife thinks I'm a genius and my 13 old son got his first instruction
in A good day, indeed. Thanks a million for your work in putting up the Web page and providing
Peace! CT |
| I found your website on the R-11 problem. This is definitely what is
fried on our Neptune. I am intrigued with your solution but not sure where
I would get the parts locally (or even where to look in the yellow pages?)
This is our 2nd board to fail so I'm willing to try anything since I'm not willing to put another $200+ into this lemon. Thanks for any suggestions. Sincerely, David |
| I just wanted to relate my experience with this issue and say thanks
for posting your web page. Yesterday, my wife told me the Neptune washer (MAH3000AWW) would no longer go into the spin cycle. I checked it out and noticesd that the 'Door Locked' indicator light also wasn't comming on. I checked out the Maytag website and found no useful information. However, I emailed Maytag with the symptoms and hoped for the best. After that, my wife did a google search for 'Neptune problems'. Your web site was one of the many listed. I am grateful to her for having made the effort. Last night I replaced the triac (NTE5657) and the resistor. After doing that, the 'Door Lock' light worked and the spin cycle returned. Then I started thinking about what might cause the triac/resister failure. Other links that came up in my wife's search, had replies from people who had verified WAX motors that had turned to shorts. If this in fact happened, it would cause the triac to blow (regardles of it's voltage rating) and in turn force the gate resistor (R11) to supply the current to the shorted WAX motor. The 3.9K quarter Watt resistor would quickly burn up. Because I didn't want a recurrence ( who knows, next time it happens it may take out the whole control board), I replaced the WAX motor. After doing a little more thinking, I incorperated one more saftey measure. This morning, I removed control board jumper JP18 (between R62 and R46). This lies just above the P7 harness connector on the control board. I replace the jumper with a 500 mA pico fuse. A pico fuse is a small fuse, similar in size and shape to a quarter Watt resistor. In the event of another WAX motor shorting, this fuse may save the triac and should surely save the R11 resistor and the control board from any potiental damage. Total expence for this repair: Triac - $2.50 Resistor- $0.15 WAX motor- $24.55 Pico Fuse- $1.00 Total- $28.20 Oh yeah, I received a reply from Matag this morning. They recommend I replace the WAX motor along with the control board. Thanks, Vince |
| My wife reported a strong smell of burning electronics coming from our
Neptune MAH3000AWW washer and a failure to spin. Since my sister's Neptune
had required replacement of the door lock and control board, I suspected
the same problem. I found R11 was completely toasted. Looking at the circuit
board traces, I saw that R11 was connected to Q6 which showed no external
physical signs of damage, but I figured it was probably dead. (It turns
out Q2 was also dead, see below.) When I googled the Q6 label MAC97A6
to try to find out what kind of part it was, your page was the first link
in the list! Searching then for "maytag r11 problem" found other
sites where I saw that some people have replaced the control board multiple
times due to this problem.
My wax motor measures around 800 ohms at room temperature on a digital multimeter, which is half what it should be. I decided to try an experiment to see if it still worked. I disconnected the wires from the wax motor and connected a power cord with mating connectors directly to it. After a few seconds the piston began to move, then there was a surprising pop and the flash of an arc inside the wax motor. However, the piston continued to extend and held the latch locked. When I removed power, the piston retracted when the wax cooled. I applied power again, and this time the piston extended without an arc. From this I conclude that there was some conductive path that had formed inside the wax to create a short circuit. Perhaps moisture was the cause, as Mike suggested. That conductive path has now removed itself! However, if I had simply replaced the control board components, this short circuit would have certainly burned out the new triac on the first use, no matter whether it was rated 400V or 600V. I measured the resistance at the moment I removed power from the wax motor, and found it to be somewhere above 3.5K ohms and falling fast. The resistance dropped to 430 ohms, then as the device cooled it slowly rose to the 800 ohm value I had seen earlier. Since the resistance varies a lot with temperature, I decided that the resistance measure is not very reliable. I next measured the current, and found it started at about 80mA, dropped to 35mA as the piston began to extend, and settled at 20mA when it reached full temperature. Since the wax motor is rated at 120mA, the measured current seemed perfectly reasonable, so I concluded that the wax motor still works. The only problem is that the design is defective such that short circuits can form and blow out the control board. Unless the wax motor has been redesigned to cure this defect, I figured that a replacement wax motor was just as likely to form a short circuit after some period of use. So, I decided to follow your idea to put in a relay with beefy contacts. That way, if another short forms in the wax motor, it can just burn itself out again. This seems like the only permanent solution. If I put in a fuse, the fuse would just blow and I'd have to replace the wax motor again. I noted Arlen's concern about needing an RC snubber on the triac if driving a relay, but there is already one on the board (R46 and C24). As a belt-and-suspenders measure with the relay installed, I did follow Vince's suggestion to replace jumper JP18 with a 500ma pico fuse to protect the control board in case I screwed up the relay wiring or (very unlikely) the relay coil should short. I'm going to put a pico fuse in my sister's machine, too, since that is a quick and easy form of insurance. After I installed the relay and repaired the control board with an NTE5657 replacement for Q6 and a new 3.9K resistor, it was time to test the repair. I selected the spin cycle and started the machine, but the relay did not actuate. I connected one probe of my voltmeter to AC neutral so I could measure the voltage on R11 with the other one. The end on the right is at line voltage. When I touched the probe to the end on the left, the relay closed! That told me the triac's gate was not being driven. Tracing the circuit on the board again, I saw that Q2 is the driver. Q2 is a KSP55 transistor. It measured low resistance in both polarities between its emitter and its base, whereas its neighbor Q1 did not, so I figured Q2 was fried, too. I replaced it with the closest match from my collection of spare electronic parts, a 2N4403. The 2N4403 is rated only 40V rather than 60V, so it might fail, but it seems to work. If it does fail, I'll find a better equivalent for the KSP55. Now the machine is back in business. For those interested in the relay addition, here are some details. The relay I found at the local electronics shop was an NTE R10-14A10-120, with 120VAC coil and 11A contacts. It has three poles when I only needed one, but that's OK. I decided to mount it on the back side of the control panel in the open space below the start/stop button (on the MAH3000AWW model at least) since both the white AC neutral wire (WH11) and the gray AC line wire (GR26) are easily accessible there. To allow lashing the relay in place with a plastic cable tie, I first drilled two holes in the plastic structure below the start/stop switch. On my machine, some excess length in the brown wire (BR14) to the wax
motor was wrapped around the wire bundle a few times near the wax motor.
I unwrapped it to allow pulling up some slack at the control panel where
I was going to mount the relay. I found the right brown wire by tracing
from pin 4 of connector P7 on the control board and pulling on the wire.
I cut the brown wire at the right spot to reach the relay terminals.
The half going to the control board goes to one side of the coil (pin
A on the relay) and the other half gets connected to one of the common
contacts on the relay (pin 7). To tap into the neutral and line wires
I cut away half an inch of insulation without cutting the wire, and
then folded the wire so I could slip heat-shrink tubing over it and
solder to the relay pin. However, using an 18AWG tap splice might be
simpler. The white wire (WH11) goes to the other end of the relay coil
(pin B) and the gray wire Cost for this repair: NTE R10-14A10-120 relay $10.49 -- Steve |
|
The resistor value of R43 is the same as R42, 18K ohms. When my R11 Burnt, it also fried my R43. I picked up a board from my local service center to determine the resistor values. Great Site.Thanks a million |
| Hey thanks for your work in putting up this site! Fixed my friend's
board after his third replacement. Didn't find your site until after I
had fixed it with parts off a failed board and was searching for the triacs.
Classic failure, just like you document. Thanks again for your effort
to help folks like me! Jack |
| I just wanted to thank you for the service that you have provided. It
was just too expensive for us to have it repaired by Maytag at this time
and I was getting tired of going to the laundry all the time. Thanks,
again. Thanks, Tim |
| Just want to let you know the information you posted is really very
helpful. It saved lots of money. In my case it saved me more than $400.
Thankyou very much. My story below will be useful for those who are not
handy enough to fix it themselves.
I didn't tried to fix it myself since I don't know enough. But I did manage to convince Maytag to not to charge me the parts. They charged me $109 for labour only. In the beginning they refused to cover any cost and quote me more than $500. I tried the second time, equipped with the new information from you web site, this time, they agreed to cover the parts. I need to emphasize that persistence is very important during with the service group, as least in north California. Again, thanks for sharing. |
| I paid .76 cents in electrical parts and 34.00 for a wax motor from
sears,2nd day shipping. This repair will work for the mle2000ayw stack
unit form sears, still the Maytag name. The circuit board is located in
the very top in the dryer unit. Maytag insist its behind the control panel.
What do they know. If you post this reply I will be glad to answer any
emails to help any other Neptune owners. Thanks for the repair info .Howard
iselloil@comcast.net |
| Thanks for posting the website.
Now Maytag will fix this problem for free! (labor and parts) in US. Call 1-800-688-9900
The class action lawsuit in US has been settled. God bless America! Where you can sue anyone for anything! (Canadians are so nice and smart.)
One day made the difference for our family. Our Neptune broken down last weekend, September 12, 2004. (First I found your website, and was attempted to fix it myself.) But I call them yesterday, they did not mention the settlement. And I called today, first there is recorded message about the lawsuit and settlement. And I made an appointment for this Thursday, they will come to fix it.
Another funny thing is that our maytag frigs light is not on, and it is not the bulb. I will offer the maytag man a beer this Thursday, but he has to use his flashlight to get it!
I donot know if they ran the same TV commercial in Canada, where the maytag repair man has nothing to do. And he was trying to beat the frig door to see he could open it before the light comes on
Anyway, thanks, and take it easy.
Bin |
| My Neptune, model MAH3000AWW, after 5 years of trouble
free service finally turned R11 to a pile of dust. Maytag was at my house
and as of today, any machine older than 5 years old will not be repaired.
Instead, Maytag is providing a certificate for a new machine. All we had
to pay was the service call of $114 to have it declared DOA.
Regards, |
| Here is some info you may want to add to your Maytag - R11 problem web site: I just finished reading the FAQ for the class action suit at http://www.maytagfrontloadsettlement.com/faq.html. It clearly covers the wax motor / control board problem. It will cover out of pocket repair / replacement expenses if they were spent before 8/9/2004. After that you must have Maytag try to fix the problem. Maytag has 1 or 2 chances to fix the machine and then they give you a certificate for a new machine. HOWEVER, that certificate is only for a *Neptune Top Loading* machine, and it's value is between $200 and $1000 depending on the age of your machine. For our '97 machine that just yesterday showed the problem, getting a $200 cert. for a top loader (we like front loaders) is just not worth it. Guess I get out my soldering iron! Rick |
| Hi,
We had the classic failure-r11 smoked and the door lock light inop.
No spin. Glad I had this site to get some background info on. Geoff |
| I found your web site while looking for ideas on what to do with my
broken maytag. I have the problem of the bearings went out after it made
a noice of a jet plane getting ready to take off while in the last spin.
I just would not spin the last spin and then I see that the door lock
ligt isn't on and the door isn't locked. The machine had an odor also.
I tryed to bing up the repair manual you had on the web but it wouldn't
show up. What did I do wrong? I want to see where to look for these parts
to see if they are burned up. Maytag will pay for the parts (up to $250) for the bearings but I don't want to pay another $175 or so for the board. Thanks |
| Guys, I came across your website while trying to fix my somewhat newer Neptune that had a severe intermittent (50%+) final spin failure. I know that your site is focused on the problems with early models but I have seen other people with this is same mysterous spin failure looking for answers. Since you have the one of the most comprehensive Maytag Neptune fix-it sites I thought you may be able to use this information. This is a copy of s post I have put out on Bobvilla and http://p204.ezboard.com/fmikemerrittmotorsfrm13 ******************************************************************************************** I have a newer Neptune MAH5500BWW. It did not have all the bad problems of the earlier models and has a modern master control board, improved door gasket, etc. However, it has had its Motor Control board replaced 9 months ago after a hard failure. So even the newer models have their warts. A month ago (early December) my wife complained that the washer was not going through the final spin properly on about half the loads. A load with 5-6 pair of jeans would never make it through. I called out the local servicer who replaced motor control earlier in the year. They came out and ran their diags, had Maytag on the phone and nothing came up, said it was probably unbalanced loads. (Note: wife was not happy at all with this!). I called Maytag service - raised hell about the lawsuit issues. They quickly sent out the motor control repair kit. The local repair company installed it. No help. Same problem. The standard 'Lawsuit repair kit' does NOT fix this intermitent spin problem! After reading up on problems and especially using the following site: www.applianceaid.com/neptune.html I decided the pump may be clogged or have something wrong with it. I removed the pump per the instructions at the webiste above and cleaned it out. There was noticable build up of some gunk in the section of the pump that had a 'boot' over a section and a red electronic device inserted through the boot. I found no other problem or foreign objects in the pump. Reinstalled pump. So far 8+ loads, including one with 6 pair of jeans, no problems. In summary: Symptoms: Fix (so far): Hint: To get to pump easier remove the motor control unit. Unscrew two screws holding unit on base and slide forward. It is not necessary to unplug cables. When removing pump. Look at how electical cables go on. They do go on in a specific way and can not be flipped. Loosen and remove hoses. Twist pump assembly from base of washer. Good luck. |
| I knew about the class action lawsuit and that many complain about the
Neptune washer, but we didnt have a problem since 1997... Last Sunday,
my wife indicated that the door popped open and all the cloths were very
wet. A second wash confirmed that there was no rise cycle.
I then found your web site and wanted to say thank you!!! I ordered the parts, including a new wax motor, decided to install another MAC97A6 & 3.9K 1/4 Watt resistor, and all is fine. (Ill have to go back and install the pico fuse.) Now I would like to return the favor. When I bought the parts, a purchased
several extras, and even if it blow s again, I wont need them
all. If you are willing to post this email alias: Thanks again for an excellent web site. |
|
Thanks for the great info. It helped me fix my stacked MUG2000AWW Neptune.
Below is the $0 -yes zero cost fix that 'works' for me. |
| My Maytag model is: MAH5500BWW which was not on your list but I have experienced the same problem that you've listed. Please add this to you list. Thanks for the information. I have filed a claim and have a repair man due here on Wednesday. Shelly |
|
Greetings Leo Dave! I inspected my board, and yes, all the smoke was let out of the R-11 resistor. The Triac was in good condition. For whatever reason, it survived. FYI, the number on the OEM Triac was HC-559C-LC in case that is useful to anyone. The factory tech says that the problem is the wax motor. It gets tired and then starts pulling too much current- BBQing the R-11 resistor and the triac. The new and improved cure for this is that Maytag has now abandonned the wax motor and has replaced it with a standard solenoid door lock. The added benefit is that now you no longer have to wait 2 minutes after the machine stops spinning before the door unlocks. And, it reduces the likelyhood of future fried circuit boards. He recommends that consumers install a surge protector in between their power outlet and the washer. He also said that the same wax motor that makes the R-11 puke is causing problems in their dishwashers. The wax motor releases the latch on the soap door in their dishwashers.... I happen to have one of these in my kitchen.... Hmmmmm..... For your information, I have the contact info and links to the claims administrator handling the Maytag class action settlement posted below. Great site and thanx for the info! Contact Info for Maytag Claims Administrator: Or send us an email at: {LeoDave: I think this link is now dead.} |
re: http://members.shaw.ca/gavb/
A friend was told it would be $400 to repair his Neptune washer and I found your page on the web. It is amazing to me -- not only have people come up with solutions, people have hacked the washer to make improvements! The symptoms on this washer -- an MAH4000AWW -- matched the page. I bought a new control board and wax motor from repairclinic.com and the washer worked! I went one more step and replaced the faulty components on the old board, along with a few "upgrades" to improve reliability, put the old board back in and that worked too! Now I'll return the new board. "control-board-in-place.jpg" shows the control board, to help people know which wires go to which connectors. What I did, all as instructed on your page: - Replace wax motor Parts: From repairclinic.com Item #: 775784 Item #: 1063620 Mouser # 511-Z00607MA 30BJ250-3.9K 576-0251.500M Net outlay is probably $25-50 with shipping (depending on how much
of a hurry you're in). Moe |
| Just saw your posting of 2/9/04 about solving your Maytag issue. I have
same problem. Not sure if you are the right person to contact, or who
Chuck is (the guy you mentioned in your notes). If its
not too much trouble, would greatly appreciate some guidance.
Though Im no electronics wiz. I might be able to get someone to help Would like to know where to get the parts (the R11 resistor and the Q6 Triac) as well as a schematic - the web site you referenced (http://mrappliance.com/corporate/repairmanual/sbrvrs/xmb_neptune_mah3000.pdf) no longer works. {Leodave: No but the link on my site still does...try it... Manual for the MAH3000}
Thanks for your original notes, and for your help, if you so choose.
Rgds,
Dave |
| Great web-site!!
I'm going to try and repair our Maytag washer using the method described by Leo. We have the stackable model, and our washer model is MHW2000AWW--can you tell me where the control board is located?? Thanks, I'll follow up on your site if I am successful. H.U. |
| We're also a victim of this horrendous MAH3000 design. It's one thing
to build an appliance that will suffer natural wear and tear and eventual
mechanical failure. But the sorts of problems this unit has are inexcusable.
Maybe these folks are the same ones who are responsible for the US vaccine
supply. Cook up a batch and test it on the entire population, then when
folks begin to drop, say "oops".
Maytag sent someone out - twice - to finally fix the mold/mildew problem in the rubber boot. Twice because the first time the plastic door insert was cracked. While they were here, why didn't they replace the controller with one that fixes the "wax motor" issue? Wax motor? What a bizarre arrangement. Why not use a solenoid on a simple R/C timer? And put the sucker on a relay or fuse the line if there's a chance of the motor shorting and taking out the switching transistor. Well, thanks to this web site (no thanks to Maytag - they refused to fix it and instead said I can get a certificate for an inferior machine) I have the answer to the question "what's the value of these charred components? In attempting to diagnose our problem I considered that the issue might be a defective door lock switch. So I located the leads coming from the switch, exposed the wiring, and jumpered them. She spins and completes a cycle but at the end the washer just keeps on trucking. It expects the "wax motor" to time out and release the door lock switch. This then allows the crude mechanical timer to advance. So for those who are brave and just want to get some laundry done while waiting on parts (refer to the wiring diagram): put a jumper between pins 1 and 7 of CONN3. This will short out the door lock spin enable switch, and your unit will now complete a cycle. For all my Red State friends, do this with the unit unplugged. Or if you only want to do this *one time* in your life, keep it plugged in and then stand on a pile of wet laundry. Be certain all your final affairs are in order. Remember: the door is NOT locked. Don't open the door until the cycle
is over, ok? |
| Hi Leo Dave:
I just contacted Maytag, and they immediately opted to give me the
certificate with no option for repair. I fought them for about a half
an hour about it, but with no effect. Has anybody out there run into
this as well and still managed to get them to cover the service and
parts? Thanks! |
| Model #MAH3000AWW I just purchased a used Neptune and can't tell how old it is. Is there something in the serial number that should tell me or some other code? Thanks. Linda {LeoDave: Sorry Linda, I just don't know...if someone e-mails me different, I'll pass it on.} |
| Model # to add to the list of Lemons
MAH5500AWW Scott |
| Hi:
I have a Maytag MLE2000AYW (Stacked!) Searched for the symptions (no spin), found your site. My wax motor reads 876 ohms room temp. About 1/2 of what Maytag states. It also works, extends in ~30 secs. But, must be bad... Found the blown Q6 and burnt R11! Photo attached. Enjoy. I was very pleased to find this site. Thanks. (Found many others also) NB: also had wax motor problem in a Maytag dishwasher soap dispenser, became very slow. (Dishwasher now gone, installed an ASKO - its VERY quiet.) Carl |
| Neptune Problem We have a Neptine MAH4000AWW that will not fill with water during the rinse cycle, it will fill during the wash cycle. I have not seen any of the web-sites that cover this issue. All of the lights come on as usual but it times out when it hits the portion of the rinse when it is should be filling with water. The only other item I can add is that the water valve quickly turns on then off before any water fills the tub, on to off is about 1 to 2 seconds only. Any help/recommendations would be appreciated. Eric {LeoDave: Sorry I can't reply to service issues, if someone sends me help on this I will try to pass it on.} |
| Neptune Motor Control issue/preemptive strike - the long story Let me say, You have a Great Board! with superb information. Now, let's see if I can help prevent some future problems with my $0.02 and maybe get somebody can give me some info. in return. First, a little background. Eight months ago, my wife and I made an interstate move to a new(to us) home with appliances that included a MAH3000AWW and matching dryer. In my naivety, I was quite pleased because in addition to fact I wouldn't have to pay to move my washer/dryer(a nice 4 year old WORKING Whirlpool gold set), a few years prior, I had seen this machine get a good write up. Well, my folks, who were local, get the Whirlpools and I get the "upgrade", and we are happy until we see the class action info. in the January, Consumer Reports. At this point my wife and I graduate to somewhat concerned but happy. February gets here, and the washer semi-croaks. We call Maytag and
find out that since our washer is seven years old, we are S.O.L. BTW, a gentlemen who answered the class action line said it hasn't been published yet, but the certificates will also be valid on a new front loader if you want to go there again. Well, I'm not one to give up without a fight, and my symptoms are similar
to the wax motor/control board/motor control problem but intermittent.
So, I find a few websites (members.shaw.ca/gavb/, fixitnow.com(now Appliantology.org),
www.applianceaid.com/neptune.html, So after too much head scratching, only one beer(big mistake not going to the store first), and staring into this thing from what I think is every possible angle, my trusty Fluke and I start into the real nitty gritty of the circuit. All easily accessible items are checking out so the frustration level is rising. I start chasing the out of balance circuit and everything still seems to be working so I'm starting to doubt my control board though all appears well. Fortunately, I decide to use my eyes and flashlight one last time. So, I stand on my head and look in the bottom back corner of the washer where the wires from the strut switch run. Low and behold, in a pile of rusty dust, two orange wires are lying against the cabinet and something is not according to Hoyle. Well, if you let a 16 AWG wire connected to a vibrating strut rest against a metal cabinet that doesn't move and add a little moisture, eventually, you will rub the insulation off your wire and occasionally short the circuit. A butt splice and little electrical tape can work wonders if you can just find the place to put them. :-) Well, I am now feeling like a genius and ready to go to the store for a sixer to celebrate. However, I can't leave well enough alone. I've been wondering about my motor based on a noise it was making, and without actually troubleshooting it, I had just assumed I had the motor control board problem mentioned in the lawsuit. Now though, I've seen the test on the service sheet that Maytag left on the back of the control board. MAYTAG SHOULD BE SUED OVER THIS!(irony intended) There a two tests. Due to strange circumstances(the wire would make up when I unplugged it from the motor to facilitate easier fluke probing) I spent half an hour to realize the following. My motor appears to be fine. However, in my Maytag, they took the wires as they start to rise up to the motor from the bottom of the machine and wrapped them in spiral wrap to hold them together and "protect" them. They then proceeded to clamp this wire bundle to the bottom of the washer With A Metal Clamp! Obviously, a spiral wrap is not a solid protective layer. The sharp edge of the clamp found its way through one of the gaps in the spiral wrap and had cut one of my motor leads into an open circuit. Additionally, it had started cutting into the insulation on the other motor leads and it was likely only a matter of time before it shorted two leads together and damaged the control board. Another butt splice, some electrical tape, and a plastic clamp without sharp edges and electrically I'm as good as new? I highly recommend you check for these wiring construction problems if you have a "vintage" front loader before they bite you or your control board. Now, since I still have my original wax motor and control boards without any apparent damage, what should I do next? The relay, surge suppressor and fuse ideas sound like good protection for the board, but can I do anything to preempt the wax motor problem? My reading seems to indicate the solenoid lock is not an option for my model. Is this the case, and if so, is there a replacement part that is supposed to be any more reliable than the original? Also, what about the wax motors in the fabric and bleach dispensers? I've seen nothing regarding these so I'm guessing they are not a common failure point, but I still wonder. Additionally, I only have slight mildew, and currently, no unpleasant odors so Im going to sanitize periodically and keep my fingers crossed unless there is another cheap fix since Maytag wont help with a new boot or door. How about an upgrade, any idea what would it take to add the temperature control feature to this machine? Is the sensor in a water valve with which I could replace the old one, or is it more complicated? Finally, are there any other items you've heard of that I might want to look into? If my machine continues to live, I may just take them up on $300 off a new machine in a couple of years(the certificates are only good for 24 months when they finally send them) or just see how long this one will last. Thanks for your patience. J. Mark |
| Neptune R11 Issue Thanks for the site! The lawsuit is in limbo, and Maytag won't do a damn thing about my dead washer. Since it's past the August 2004 cutoff date, no reimbursement for repairs is available. I have a model MHW2000AWW washer, which is not on your list, a stacked unit. (Like a certificate for a top loader would do me any good anyway?) The Claims Administration company told me I could wait a few months until the settlement, then Maytag *might* fix the machine. Yeah, right. Per your site, I replaced R11 and Q6 (which looked fine, but I went with the 600 volt replacement anyway). I also replaced the Wax Motor. It was a challenge finding the control board. I finally found it in the top of the dryer after dismantling much of the stacked units. It turns out all one needs to do is remove the two screws on the top cover at the front of the machine and pull the front panel of the dryer out and down, hinged at the bottom, to find the control board in the upper right. A couple of screws hold it in from the top of the dryer. The Wax Motor is accessable by removing three screws from the panel separating the washer and dryer. I used a screw driver and needle nose pliers to worry the spring holding the wax moter in place out, then I could remove the motor. It's resistance was 800 ohms, while it was rated at 1.07K. That would explain an increase in current throught the resistor, I suppose. I ordered a new one, and received one rated at 1.135 K ohms. My washer is back and running for less than $20, and that is significant, as the repair for this $2K combo would have been a lot more! I think I'll buy a few more wax motors, and treat this washer like my smoke detector, and replace the wax motor every year. I figure I can afford $14/year for a wax moter every year much better than a new stacked combo! Oh, and this lawsuit has cost Maytag $33.5 million so far, and it's not over. I'm also advising everyone I know not to buy Maytag. I could go on and on... Again, thanks for the web site. Larry R11 Issue. (Part 2) Hello, This is my second email. My first detailed my experience. I understand that the only consensus that the wax motor is the source of the R11 issue is with Maytag. However, I'm leary of coincidences, and my wax motor had 30% less resistance than when I bought the machine. If the wax motor is the cause, than a cheap solution could be a resister or potentiometer in series with the wax motor to offset the loss of resistance in the wax motor. Again, thanks for this site.. Larry |
| Maytag R11 and Q6 Problem Good day. Thank you for the valuable information provided on your site (http://members.shaw.ca/gavb/). With the information I found on your site I was able to save several hundred dollars in repair costs on an MAH400AWW Neptune. Unfortunately I found your site after I had already purchased the Technical Manual and Wax Motor from RepairClinic.com. I consider it a small price to pay considering I can probably reuse both in the future. I had a devil of a time finding the necessary parts for the control board. In the metro Atlanta, Georgia (USA) area I found 4.7K Ohm resistors
(carbon film of course) at my local RadioShack (5 pack for $0.99). I
checked with an electrical engineering friend and he advised that the
4.7 would be fine to replace the R11. The Q6 Triac was more difficult
to track down. I found it at ACK Radio (http://www.acksupply.com/).
If this problem recurs I may install the pico fuse at JP18 and the in line fuse above the wax motor. Thanks again to all who have contributed. Brett |
| The fine blown R11 Ya know you gotta love the Internet if not for some of the BS the open ability to make your problem known is the best!... I Suffered a motor controller/motor replacement about 1.5 years ago. Today I went to get the wash out of the washer and the timer was stalled in the middle of the cycle. I just figured A power outage was the cause. I pressed the start button the washer started going and AHH yes all is well (or so I thought). 2 hours latter I return to find the same thing along with, the all to familiar smell of cooking semiconductors in the air. I pulled the washer apart found R-11 cooked checked all the coils fed from the control board which seemed ok. Now the good part how do I figure out the value of R-11. I have to say I was kinda pissed after fixing this machine once already. Your site quickly put me at ease thanks for taking the time to post your (and everyone else's) findings. Now I have learned about the law suite so I will file a claim to get back my $$ for the drive motor and controller and tomorrow I will place a call to maytag to come replace the main controller and get rid of the wax motor... once again THANKS..... Kevin O |
| Neptune MAH3000 control board schematic Hello!
I just experienced the wax motor short and the R11 fire along with
the Q6 pop. I am now having water fill and timer problems, like it doesnt
fill and the timer is balky (most likely due to the water issues). I
replaced the 4 triacs, but problems still exist. Are there resistors
to change as well?
Thanks! Bill |
| Maytag Neptune Hey, thanks for your site. I have the MAH4000AWW model Neptune front loading washer. It's a few years old now, and for the most part I've had pretty good luck with it. I did have a repairment out under warranty in the first year to replace the front door boot due to a small leak. Since then, it has had the mold/mildew problem and I had joined in the class action lawsuit. Then several weeks ago, the spin cycle stopped working. I noticed the door lock light wasn't coming on, and then reviewed the class action material and realized I was just experiencing both problems now. After searching the internet I found your website. THANKS! I pulled the control board and found my R11 fried. Well, I was going to try repairing it, but then thought about "Ben's" comments, and gave Maytag a call. They authorized not only the replacement of the control board, but the replacment of the door seal as well. Even let me keep the old board, which I'm still going to repair to keep as a spare. (Now, if I can just find the parts around here without having to buy a large quantity!) Also got to keep the seal. Cleaned it up by soaking it in bleach, and I'll keep it also as a spare. BTW, repairmen told me the best way to keep that door seal from getting mold/mildew, is just to run some vinegar in the rinse cycle now and then (about the same amount as you would use of Fabric Softner...just put it in the Fabric Softner dispenser, and don't use the softner!), or to spray the door seal with bleach occassionally. Also said it helps to keep the door open when not in use... He also recommended replacing that wax motor every few years. Colby |
| R11 & Q6 problems fixed thanks to you Thanks for saving me a bundle of money! It's Feb. 11/05 and 2 days ago, my Neptune MAH4000 refused to spin at high speed and the Door Lock light did not come on. I guess I've been one of the lucky ones since this is the first time it failed since I bought it in Dec 99. I called Maytag and they said that they would not service it free of charge. They said I had to pay for the labor & parts and then submit a claim form to the class action lawsuit. The lawsuit states that they may at their election, make a repair attempt or simply give me a $500 coupon towards the purchase of a Neptune Top Loader. After questioning them at length about this, they said they would not pay for any repairs. All I would get would be a certificate for an overpriced new washer. Since the repairs from Maytag would cost $400, and I had no idea how
to fix the problem myself, I started thinking about just buying a new
washing machine (NOT one from Maytag!). In my search to find opinions
of washing machines I came across many sites of furious Neptune customers.
Today, I replaced the wax motor, R11, Q6, added the inline fuse and my wife is pleased as can be with a fully functioning washer. All for less than $25. Thanks again for your help. It really made my day! |
|
I am very confused. My washer will not spin and no locked door light
is on. I have a soaked load sitting in the washer. My washer was purchased in '99 and it is a MA3000. I need a washer
now,. |
| Greetings, I just wanted to know if you have had any problems with Roy's answer to the problem by using higher voltaged capacitors. There was a different opinion from an e-mail by mike, but I think that one e-mail seemed to kind of go unnoticed that seemed a really good idea. A guy named vince installed a pico fuse which should blow, and save the circuit board. 1) Has anyone tried this and 2) Has this solved Vince's problem. So I guess before I jump in with both feet, I am interested in trying Roy's solution with possibly Vince's little addition. Thanks for any info in advance, Sincerely, Dave S. {LeoDave: no responses yet...will post here if get one} |
| Hello, We have the MHW2000AWW model. It's a stacked unit with electric dryer. Blown R11, replaced and blown again despite new wax motor. Glad I found you, thanks for all the hard work you and others have put in. I have seen two solutions by Roy, one on your site and one on an email thread, I would like to know which is most current; 1) You do not recommend repairing the board. I do, with qualifications.
1: IF! The board has not been seriously burned. and The second is on your site, which do you recamend? John |
| Hello Leodave- I am very grateful for your web site and the responses you have posted. All have been incredibly helpful. I recently lost the spin on my 3000 machine after seven years of excellent service. Of course no help or interest from May tag and the insubstantial certificate offered. From your info, I immediately found the R11 burned, but Q6 appeared intact. I replaced the R11, Q6 and added the pico fuse at JP18. Still no spin and nothing re-blown. I checked the wax motor and surrounding parts, all appeared ok, but I figure the wax motor must be shorted completely. I taped down the black button on the Door Lock Spin Enable Switch. This allowed the spin cycle to run (yea!). I then tried this with the wax motor disconnected - no spin this way. I reconnected the wax motor and normal spin returned. I also tried running the machine with the door lock mechanism shut (white plastic hook) open or shut made no difference in the spin cycle with the button taped up. The machine runs a complete cycle and stops correctly; I only need to push the on/off button to turn it completely off. I have no knowledge of circuitry, so I don't know if taping the DLSE switch would work with out replacing the R11 etc, since that it the first thing I did - I think probably not. Maybe this will save someone from buying another wax motor if one is not readily available. Again thank you so much for the information - Respectfully - Kristie |
|
Here's my take on the design and issues. We had the same R11/Q6 problem
- after 7 years, but the service guy just replaced the control board
about 6 months ago as a matter of course when replacing the boot with
mold buildup. Mike |
| I've got a MAH3000AWW that doesn't spin, and read with interest your
solution and every one of the e-mails on your page. My machine commits
HariKari instead of spinning. It shuts off before the last of the water
is pumped out. When you push the start button, the water pumps out but
the on light does not come on, and the machine quits as soon as you take
your finger off the button. Before I got to your page, I had determined
that both the switches (door lock indicator and spin enable) were ok.
I replaced the wax motor even though it metered 1800 ohms, give or take.
When I opened it, it was scorched inside, so probably a good thing. While my R-11 and Q-6 looked ok, an e-mail said maybe the Q-6 is shot, so I replaced it with a 600V triac, leaving in the R-11, which metered 3700 ohms, give or take, up to specs. No problem to replace the Q6. Except just no results. That's right, the thing still wouldn't spin. I tried fooling the machine by holding in the door light control, holding down the inner door latch, and closing both the door lock and spin enable switches, while pushing the start button with the machine set on spin. No good. So I went back to square one, using the troubleshooting sheet that came built into the machine. It passed all the tests until I ran across this sentence there: "...if you have continuity between the spin enable switch and connection P3-7, replace the control." Is this another sample of Maytag's ineptitude? The continuity from the control to the spin enable switch all takes place south of the control, so why replace it if the wire is in one piece?? Anyway, if anybody out there sees this and has a suggestion, I'll give it a try. I had to buy a $10.00 minimum and pay $5.00 shipping (Ack), so I have a few 600V, 0.6a triacs (MAC97A8) that I will sell for $2.00 each postpaid. Also some 600ma Buss 5x20mm fast blow fuses (GMA-6/10 BUS), also $2.00 each PPD. If you want one of each, which was all I needed, just send $3.00. (May/05) Contact goneape@hostgorilla.com There's a page with the resistor codes here: Thanks for the page Leodave, and if you're paying to have it hosted, contact me, I'll put it up for free, no strings. -Chuck |
| Great site. Have replaced R11 & C-6 and once again have 120 VAC
at the wax motor leads. Still awaiting arrival of a new wax motor (original
had only 930 ohms resistance), but am sure I'm back in business. Less
than $40, with $15 shipping included. The one thing I couldn't find on
the site was a picture of the opened
door latch assembly showing the wax motor, so I include one for posting
if you see fit. Thanks again for the help! Jim |
| Hi, Thanks for the website it is a lot of help. I've replaced the wax motor, resister, and triac on my neptune washer and the door lock started working. I thought great, until I realized, it now won't unlock. :) I was just wondering if you'd had any emails from anyone else with this problem. I've been researching it on the internet but can't find anything on it. Again thanks for the website, it was very useful. The only thing I did different was I replaced the Q6 triac with an 800 volt instead of 600 as our electronic store did not have a 600. I don't think this would cause the problem, but I really don't know. Any feedback would be greatly appreciated. Thanks, Brian |
| I purchased the Maytag Neptune Washer (MAH3000AWW) and Dryer at a yard
sale and it worked fine for about a year then 2 weeks ago it stopped spinning.
Thanks to google and internet searching I came across your web page and
thought what an easy fix. So I called my Dad (who is an electronics technician)
and said can you do this? Of course it was an easy fix, though finding
the NTE 5657 was hard, we ended up locating an NTE5656 and replaced that
along with the resister and it worked. We are now ordering the NTE5657
to have on hand in case this happens again we will be prepared.
Again I wanted to say THANKS for saving my yard sale find. Tamara |
| Hi, I have a model MAH5500BWW. Of course, the door wouldn't open and it had stopped mid cycle with clothes in the washer. I found out how to open the door from Maytag.com. Very simple. Hope this helps someone else. On my model, I removed the four screws that hold the soap dispenser. Lift out the bleach and softener tray. There is a green cord that looks like a weed eater string that is located towards the front of the machine. I had to feel around to find it but, it was there under the top front of the washer. Just give this green string cord a sharp jerk and you can open the door. This saves the expense of buying a new latch. Now if have to take the advise of replacing the Q6 and R 11. I am in my mid 70's and female. If I can do this, so can you. Hope this helps someone. Carolyn from Oregon |
| Hi there
I came across your site while looking for info on how
to mix my Neptune Dryer. Its a Model MDE5500AYW and it has what
I believe to be a faulty door switch. All this lights etc work
but
no actual drying occurs. I have a call into a local service company and
have a replacement door switch on order ($6.99). I was wondering if you
had any idea on the difficulty of fixing this myself.
Thanks for any info!!
John V |
| Hi-
I recently replaced the spinner ball bearings in my Neptune MAH3000,
but have had no other problerms. At that time I also added a 500ma fuse
to the wax motor as per M. Little. Off hand, have you heard of anyone
who has also done this and has had the fuse blow? In other words, does
this fuse actually protect the control board (R11, etc.)? Dave:
I'm sure it helps Thanks for the great & useful web page!! Dave, H |
|
Hey, your solution works. We have a Maytag Neptune MAH3000AWW and have
spent more than $500.00 over the past few years on this miserable machine.
The repairman immediately knew what the problem was, but I was reluctant
to spend another $250.00 plus for the wax motor and the board, especially
for a 2 cent transistor. I tried to get away with replacing the transistor
alone, but ended up replacing the wax motor, R11 resistor, and the Q6
Triac--Walla! The door locks, and the machine spins for less than 40
bucks. Your website saved us a bundle, and I suspect that the 600 volt
Q6 will solve the problem indefinitely. Ralph.W., PhD, Redding, CT. |
| I really appreciate the info. I was the proud owner of model mah4000aww
Neptune washer until yesterday. Repair guy came out today and quoted me
$380. I told him to forget it after he told me over the phone that it
was a circuit board problem. I removed the board myself today. Thanks for the information. Maytag should mail out a notification. Thanks, Jeff |
| I just want to add my thanks for your time in putting together a very
useful website. And an extra big thanks for the pdf manual! Unfortunately,
my Neptune blew out the tub seal and water destroyed the bearings. They
made it so the bearings are not replaceable by themselves, but I guess
this is a trend in almost all new washers.
Mark L. |
| Hello Leo Dave: I just want to say thanks for your having this website. I bought my MAH3000AWW washer in October 1997 and didn't have any problems with it until a few weeks ago (October 2005) when the wash would tumble but not spin. After opening up the back panel, one of my housemates spotted the fried R11 resistor. We then did a search on the internet and found your site containing all of this helpful information. I first contacted Maytag and was told that this problem would have been repaired free if I had submitted the class action papers by a certain date which passed. Since I didn't want to buy a new control board and wanted to see if I could repair the board myself, I then replaced the R11 (3.9 kilo-ohm) resistor and the Q6 triac with an NTE5657 part both of which I found at the local Fry's Electronics store (in California and Arizona only). The washer still did not spin, so I then ordered a wax motor from Marcone (a chain of appliance parts stores), and this took about 1 1/2 weeks to receive in the store. After installing the wax motor (with much help from a copy of the service manual (found on your website) which described how to remove the front panel to get to the wax motor), the washer still did not spin, so I thought the Q6 may have been blown again, so I replaced this with another NTE5657, and still the problem was not fixed. Finally, I followed the advice of Steve (on your website) and replaced the Q2 transistor. Instead of the 2N4403 part Steve used, I found a 2N5400 transistor (in a TO-92 package) from HSC Electronic Supply in Santa Clara, CA. This is a 120 volt rated part (much more adequate than the 60 volt rated original KSP55 part). The washer finally spun after making sure it was in the spin cycle for at least several minutes! Thanks Steve for your helpful advice. If this last fix did not work, I was ready to buy a control board I found on EBay at a starting bid of around $10. Apparently, there are many Maytag control boards for sale on EBay, so I think it's worth a look instead of buying a brand new one for almost $200. Mark: Thanks for your advice about jumpering between Pins 1 & 7 of Connector 3 as a temporary fix for latching the door lock. However, maybe we should leave politics ("For all my Red State friends, do this with the unit unplugged.") out of this. Thanks all for your useful comments. The internet is a wonderful forum.......... Joe in Mountain View, CA |
| LeoDave,
The solution sounded sooo easy. Only to find out that my board doesn't
have a Q6. The fix to the spin cycle/no door latch light problem was
right down my symptoms. The wax motor measured 1200 ohms cold and 1500
ohms hot, it started extending at 55 seconds, with a small click, fully
extended at 100 sec. The new wax motor measures 1000 ohms cold and 1500
ohms hot, it started extending at 35 seconds, fully extended at 60 seconds.
(far from the 1900-7200 ohms specified). So I removed the motor contol
board, only to find that it didn't look like the one on your web page.
No Q6. Nothing shows burnt. R-11 looks good. My Motor Control PC shows
like the one at mlittle.com/appliance/neptune Model AA19680, P/N 6 2702240,
ID 225622908. Any help out there? (If you can help email LeoDave and I'll
forward to RJ, Thx Dave.) Great web pages.
From: Ken RJ, who is looking at the "motor control" board, found that R-11 looked fine and he couldn't find Q-6. Thanks Leo. Your forum is helping a lot of people. We need more people in the world like you. Thanks again, |
|
You are one heck of a great person to go through all of this for us
Neptune owners. Pathinton@..... Thank you for taking the time to email, that makes it all worth while...and I'm sure there are a quite a few happy people out there who don't email me too. :-) |
|
Owners Solution to Mold and Smell Problem in Neptune I own an MAH4000 that I bought about six months ago at a yard sale for $75.00. When I tried it I found that it was filled with mold and would not spin. After reading your excellent website I replaced the R-11 resistor, the Q6 triac and the wax motor. I also protected one leg of the wax motor with an AGC-1/2 fuse. So far the machine has run flawlessly. I solved the mold with a 2 step approach. I first sprayed about 1 quart of pure bleach into the door seal and drum of the machine, shut the door and let it sit in the garage for about one week. When I opened the door about 99% of the mold was gone. When I looked closely there was still mold down in the pores of the door seal, but none actively growing. I might add that this machine had not been upgraded with the new type door seal kit. The mold was very minor at this point, so I took the machine upstairs and put it into service. We were thrilled with how well the machine washed our clothes and both decided that if we could control the mold and smell problem we would keep the machine. Initially I would check the machine daily for mold in the door seal and target any I found with a 50/50 bleach and water solution. We also take a towel and dry out the door seal, door, tub and the soap/bleach/softener dispenser area every time we use the machine. We keep the dispenser area spotlessly clean. We leave the dispenser door and the washer door open all the time. There is absolutely no mold growing in the door seal of our machine. Rachel is extremely sensitive to allergens but has no problem with the clothes washed in this machine. It smells fresh and clean inside. I now check the machine about twice weekly but I continue to find no mold and have not even had to spray the door seal with bleach. I think the key to solving the mold and smell problem is to keep it dry and leave the doors open when not in use. I also plan on replacing the wax motor yearly as insurance. It only takes about 5 minutes to replace once you figure out how to get to it. I hope this helps folks who own these machines. It has solved our mold and smell problem so far. Rachel G.
|
| ... or was it MHS2000AWW? I don't really remember. It's about a 5 or
6 year old stacked neptune.
First of all, thank you so much for the information. My wife was pulling her hair out once our washer headed south. It's unclear to me whether this came before, during, or after our dryer plug and outlet fried. A few things I thought you (or your readers) might be interested in: (+) Always be sure to unplug your unit before disassembling it. Just a reminder. (+) On the stackable neptune, the main controller board is attached
to the top of the unit. Took me a while to find it. Easiest way to get
to the board is to undo the 4 screws on the top of the machine. (+) Again, on the stackable neptune, the wax motor is hidden behind a panel just above the washer door. The easiest way to get to it is to first undo the two screws (one on each side) on the slanted panel just below all the controls. Remove this slanted panel and you should be able to find a screw pretty much in the center of the unit, just inside the lip you just exposed. Mine was underneath a bundle of electrical cables. Once you unscrew this, you should be able to lift out the panel that covers the wax motor. (+) I've never soldered anything before in my life, but was able to do this reasonably easily. (+) In the SF Bay Area, you can find the necessary parts at R & D Electronic Parts in Milpitas. Interestingly enough, they even had a printout of your webpage behind the counter. I was asking the guy about the NTE triac and he said, "Neptune?" I had to chuckle that he knew exactly why I was looking for the part. I love the internet. :-) Cheers, {LeoDave: Just getting your e-mail made my day LOL, makes it worth the effort. I would love to know how many other shops have my webpage posted up? and thanks for taking the time to add more useful info, I don't get time to reply to every e-mail, especially the ones asking about other problems as I am not an electronics or appliance expert, but posting this into the feedback doesn't take long and benefits so many other... hope your fix last a while...I added the surge protector, sounds like you might be wise getting one too...have a great day, every day. Cheers, Dave.} |
| I bought the Neptune Nightmare back in 1998. All was running well until
last year (2005) when I had my first Neptune experience. For the previous year I discarded the postcards and letters warning of impending doom with the class action lawsuit. Figuring it was a case of lawsuits run amok. Last year my Neptune stopped draining and all I could think is oops,
I should have listened to I located the three screws on top of the machine, removed the cover
to get at the control board expecting I undid the four screws on the door and pulled off the front panel.
With mirror and flashlight I was able to get to the little I removed the wire and everything was back to normal. I went back to
thinking the lawsuit was a lot of bunk and The washing machine stopped draining again. After grilling my wife
and getting a full accounting of all underwires, I A few clicks to mouser.com to get the resistor and another to repairclinic.com
to get the motor and four days Thanks so much for your website, a true public service! Regards, {LeoDave: Jan 2006 - Thanks
for taking the time to write Tom, I enjoyed that one |
|
Source for Parts for the Maytag Neptune I'm probably just one of thousands that you have helped save hundreds. I want to say thank you. My biggest challenge was finding the parts, so I thought I'd contribute the online store that I used ... for the good of the cause. I only needed to replace the Rll and the Q6. You'll have plenty of resistors left over, but I wouldn't grouse about "wasting" a few pennies when it saves about US$3000. Shipping and handling cost will be about double the actual parts cost. The vendor that I used is Unicorn Electronics located at http://www.UnicornElex.com/. Here are the parts that you need: NTE5657 Triac-600VEM 0.8A 3.9K Ohm 1/4 W Carbon Film Resistors 50 Pack Item #: 10-8086 Thanks much, - Scott |
| Good morning. Below is a summary of my model and problem.
I was able to fix the board for $32.79 CDN taxes included (instead of
$317.95 plus taxes for a new board), thanks in large part to the information
on your site, and a good service person. Thanks! Rob L......, Orleans, ON Canada Quote of the Day Nothing deters a good man from doing what is honorable. Seneca Maytag R11/Q6 Problem Q6 Triac NTE 5657 $6.64 |
| My issue was a little different in that the door lock still operated just fine. However the motor would not engage spin or regular tumble cycles whatsoever. anyway, thank you for such a great site. Unfortunately I did not find this site until AFTER i paid Maytag for the service call AND a new controller board/washer motor. Why they make the motor's harness soldered directly to the control board is beyond my comprehension. I did read about the class action lawsuit, but apparently it does not matter any longer as there's an expiration on the suit? How can there be an expiration? the exact same problem occurred. What does irritate me is when I called up, the rep stated that parts were covered and it would only be the cost of the service call. The technician stated that was not the case. Ah well, I was never good at haggling :-( If you'd like pics of a fried MAH5500BWW board, let me know and I'll be glad to snap a few. Dan |
| My Maytag recently went out and I saw your site! My question is whether to replace the Door Wax Motor or not as well as the R11 and Q6 Triac. If I don't replace the wax motor will the same problem occur again? The washer starts to run then stops and the door latch light is ON. Thanks for your help, {LeoDave: Feb
2006 - Kyle, (and anyone else) Yes, I think the recommendation it to
change the Wax Motor. |
|
Ran across your site. Read up on your fix. Went to R&D Electronic
Parts in Milpitas, CA to get the components. Got the wax motor at APED
appliance parts in San Jose, CA. I called a friend who knows components and he replaced r11 with a 1
watt behemoth and the 600v triac. We replaced the wax motor and turned
it on and the first thing I noticed was that the door lock light came
back on which was a good sign. It seems to be back up and running. Thanks so much for your help. It was going to cost about $400 to have
it done by a Maytag guy, the control board/wax motor was going to cost
$180 if had just swapped everything out myself. As it was, the total
for the wax motor and components was less than $30. All I can say is awesome. Thanks so much. Michael |
I purchased the subject machine from a coworker for $50. He said it wouldn't drain. I quickly learned that it wouldn't drain the glycol balancing solution in the balance ring on the front of the drum! I ran across your web postings and became aware of the class action suit while looking for wiring diagrams, etc. I found the classic R11/Q6 problem and replaced the components per your instructions including a new wax motor and an inline 500ma fuse. Since he claimed that the motor ran fine I was disappointed when it kept tripping off! Further investigation found the motor control board fuse blown. Maytag service manual says don't try to repair, just replace the motor and control board.
Instead, I replaced it with a fuse holder and a 10amp fast blow fuse, then ran the motor phase tests and found that there were other problems on the motor board. The motor phase continuity and wiring was good. I searched for motor board repair info and found none, so I pulled the board and started doing some continuity/resistance checks. I started with researching what and how MOSFETs work. I checked forward and reverse resistances across all combinations of terminals on the MOSFETS and tabulated the results, looking for differences and trends. When I finally got to the A-phase MOSFETS the resistances were zero. I wasn't sure if the short had affected the Hi/Lo driver and resistances on them weren't conclusive. I decided to spend a few bucks and attempt a repair, while purchasing a Maytag motor conversion kit on Ebay for $100 + shipping ($22). I went to Newark InOne's website (www.newark.com) and ordered six replacement MOSFETS and three Hi/Lo drivers (plus 10 600v Triacs for machine board spares). I chose IRF740 (400V) MOSFETS at $1.27 each and exact replacement IR2101 drivers at $2.27 each.
I decided to first replace all six MOSFETS and leave the drivers alone (only two were bad). I disassembled the board from the mounting bracket and used the soldering station at work to cleanly remove the old MOSFETS and resolder the new ones in place. When I inspected the under side of the board at the A-phase end I found evidence of a short, probably caused by moisture between the MOSFET terminals. After reassembling and installing the board, the machine runs fine! I didn't need the drivers, so I have spares. I also received the motor upgrade kit just in case my fix later fails, but it has been through a month of laundry trials so far and is holding up just fine.
Oh, one other note. The Maytag service manual is in error relative to the 24VDC tests on the machine board. You need to test for 24VDC between the P4 pin 3 and line on the line relay not neutral on P5. This was really throwing me a curve, as I thought my machine board control power supply was bad.
I am so happy with my $80 washing machine that I bought a new Neptune dryer to go with it!
Hope this helps someone else save some money,
Bill |
From: matt [mailto:boscosvids@hotmail.com] {LeoDave: Feb 2006 - Can anyone help Matt? Please send him direct as I do not own a maytag anylonger I can't take a look., Thanks} |
From: NJ Star [mailto:njstar9@sbcglobal.net] Hi Leo, I came across your site while trying to fix my washer. The motor does not spin. I found a wiring diagram from the back of the console, ran some test, and found some fried parts at the motor control board. 10 amp fuse, Q5, R34, R35. So far I have bought the fuse. I am planning to buy the rest from radio shack, but I need the values of R34 and R35. I'd be much appreciated if you can provide the resistance values or a full schematics would be great.Thanks in advance.
Best regards,
NJ {LeoDave: Feb 2006 - Can anyone help? Please send NJ direct as I do not own a Maytag anylonger I can't take a look., Thanks} |
| I am so happy to find your site and realize that I am not crazy - Maytag is no help at all. I have a door latch and wax motor problem (I am sure of this after reading all the postings, and I look for the $-11 and yes, it is burnt out). My question is - any of you genisus' live close by and would like to try fixing my machine before I replace it? I'm totally intimidated by all the welding talk! I live in the Clinton, NJ area! DorisDSZ@aol.com - Posted: 24th Feb 2006 |
I'd just like to say thanks for the information on how to fix my Maytag piece of crap washing machine (in my opinion). Works again after the R11 & Q9 replacement. I also added a 500ma fuse in the J18 position. Boing - Posted: 26th Mar 2006 |
From: Larry Anyone find where schematics on these boards can be found ? More than likely they are confidential not for release. Larry {LeoDave: Apr 2006 - Can anyone help? I have a manual PDF on the main page but nothing else. Please do send me anything and I'll post it as soon as I can with a link on the main page, Thanks} |
From: Josef D. I just want to thank you for your very informative forum for saving me a bundle in making my own repairs to our 6 years old MAH3000AWW. Joe |
From: Magnusen
Sent: June 24, 2006 9:52 PM Subject: My MAH5500AWW Hi and thank you! When the washer started showing problems, we were only two months into our new house. The clothes came out soaked, so I deduced there was a problem with the drain pipe, drain pump, or the controller for the drain pump. I cleaned the drain pipe and I ordered (from RepairClinic.com) and replaced the drain pump. Obviously the problem wasn't solved. I emailed the RepairClinic.com guru and asked if I should look for anything else before replacing the board and he clued me in to looking at R11. That's when I found this site.
After spending an hour reading and pulling the circuit board out my washer, I ordered 3.9 kOhm resistors (R11) and MAC97A6 triacs (Q6) from DigiKey.com, and a new wax motor from RepairClinic.com. I also shipped the old drain pump back to RepairClinic.com. At first, I just replaced R11 since Q6 still looked like it was in good shape. The new R11 cooked instantly. Since R75 was showing some damage (the stripes were burned on the side next to R11), I thought I should replace it too. I took my 6 year old daughter with me to Radio Shack and taught her how to order the resistors. When asked "what can I help you with today?", she spoke up and said "Resistors! 10 kill-a-gnome and 3.9 kill-a-gnome!" He laughed. Back at the washer, I replaced R11, R75, Q6 and replaced JP18 with a 500 mA fuse. The washer is 4 for 4 as I type – it all works again.
I really agree with "Mike's Info" over "Roy's Info", but both are insightful. The triac drives the wax motor, but can only do so if the motor is well behaved. When the motor fails, the R11 and Q6 circuit elements overheat and fail.
Before the washer can go into a spin cycle, it locks the door so wet clothes don't come flying out if something is out of balance. The Q6 triac applies a little current to the wax motor, and it heats up an element inside ("goo" according to Mike) that expands and pushes a short rod to mechanically get the door locked using a series of gears. Part of the lock includes a detection circuit to verify the door is truly locked. If the door isn't locked, the spin cycle is cancelled and your clothes sit there full of water. I've been wringing them out by hand in the back yard before tossing them in the dryer.
So, the wax motor for the door lock is the key. Over time, it heats and cools, heats and cools. The overall resistance, around 1.8 kOhm fresh off the shelf, drops over time. Some of the people at the site said they measured their old one at less than 900 ohms – half. You see the rest: the motor's resistance drops with age, the current through the triac and R11 goes up, and eventually out comes the magic smoke. The fuse needs to be there. If the motor ages poorly again, the fuse will blow before any components get cooked. I'm going to order another couple wax motors soon, in case they stop production and I have another burnout in 5 years. If the fuse blows, that means the motor is gone. So I only have to replace a 9 cent fuse and a $17 motor without getting out the soldering iron again.
When I called Maytag about this and said I had the same problem as everyone else in the lawsuit, the "customer service representative" audibly shivered and immediately read me a prepared speech about how the deadline for repair or reimbursement had passed, how they had dutifully sent letters to everyone who had filled out their registration cards (I didn't) and how they advertised in USA Today, etc, etc, etc. She refused to talk to me at all after that. I wasn't going to argue with a supervisor, so I hung up and started ordering parts online. All said and done, I'm out about $50 for doing it myself - that's a little over a tank of gas these days.
Thanks again everyone, and especially to Leo Dave for the website! Todd {LeoDave June 2006: Thanks Todd, it makes it all worth while loading it up when I recieve emails like yours, and I'm sure Maytag love my site too LOL }. |
From: Marilena
Sent: May 17, 2006 9:39 AM Subject: maytag problems... Hi!
I just found your site, and I
started to have some hope… My Maytag Neptune washer (I think it is a MAH 4000…),
which gave us many, many headaches ever since we’ve got it, like 5 years ago or
so, now it is not extracting the water from
the clothes anymore… it gets to the end, I go to put them in the
dryer, and they are completely soaking wet, doesn’t matter what I tried (put on
the spin cycle again, etc.). Is this problem fixable, and WORTH fixing – or
should I be thinking about cutting my losses and buying another washer (which is
going to be a big blow to our budget…)?
Thank you so much for all your
help!!
Sincerely,
Mary
|
From: Robert
Sent: June 26, 2006 10:37 AM Subject: Maytag No Spin Problem - Alternate Solution
This solution is applicable as long
as wax motor is not burned out or shorted across its terminals. It will
implement door lock and lock light. OBSERVATION: Bob |
From: Henry Thanks for all the info,
|
From: Steve
Sent: August 2, 2006 8:47 AM Subject: Another opinion on Q6... A lot of the focus has been on the breakdown voltage of the Q6 triac (400 volts vs 600 volts). I don’t think that’s the issue. I believe the key is the current handling capability of Q6. A triac is a solid state switch, and in this circuit it is being used to supply 120 VAC to the wax motor. And what happens is that as the resistance of the wax motor drops (due to age and intermittant unreliability of the device), the current through it rises: I = V/R. When the current exceeds the rated capacity of the triac, it blows. The suggested Q6 replacement device, the NTE5657, is rated at 800 mA. So the load resistance that will smoke the 5657 is R = (120 / 0.8), or 150 ohms. That means at 120 volts, if the operating resistance (R under load) of the wax motor ever drops below 150 ohms for more than a few milliseconds, the 5657 will blow.
Notice that R11 is not in the high-current path. It is there to protect the gate terminal of Q6 from being over-driven. But when Q6 blows due to too much current, it sometimes (usually) shorts back through the gate and this lets the high current bleed back through the gate and that blows R11. When this happens it often blows the driver transistor Q2 as well.
So my latest experiment is that I am substituting the NTE 5645, which is a high-power triac designed to sustain 10 amps. It can also handle a surge of 110 Amps, so it might even be OK with an arc flash-over in the wax motor if it’s over with quickly. The wax motor resistance would have to drop below 12 ohms in a sustained fashion to blow this triac. It also has a 600 V breakdown but I don’t think that is a concern in any case – the voltages in this circuit are all in the 120 V range.
The reason I am going this route is because I have already replaced Q6, R11, Q2 (also blown) and the wax motor. This fixed it for about 2 months and then it blew again. One solution that has worked for some people is the relay modification. But a high-power triac is the solid-state equivalent of the relay circuit. The advantage is you don’t have to modify the circuit or cut leads. This should work. All we’re trying to do is figure out how to handle the intermittant high current that these unreliable wax motors seem to draw down every once in a while. Higher current handling capacity seems to me to be the key to accomplishing this goal.
Obviously the control board can’t sustain these current loads for long in any case – the wattage would start melting components. The drawback would be if these higher currents are sustained for very long, they may smoke the circuit traces on the control board. I’ll let you know if that happens. I’m not replacing my wax motor this time. I think that’s a waste of time and money. And if it blows the circuit traces that carry this current I’m just going to replace them with wire. Right now I’m going on the theory that the wax motor resistance drops into very low values intermittantly but then returns to sustainable values. If I’m wrong, at least the result will be interesting and informative. Steve |
From: gregory |
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Yeah - Right!
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